ORIGINALLY PUBLISHED IN
"GUITARMAKER", ISSUE #84 SUMMER 2013
THE JOURNAL OF STRINGED INSTRUMENT CONSTRUCTION & REPAIR
PUBLISHED BY THE ASSOCIATION of STRINGED INSTRUMENT ARTISANS
STRATOCASTER
RESTORATION
By BRIAN HOWARD
WWW.BRIANHOWARDGUITARS.COM
With the value of
vintage instruments skyrocketing, guitars that were considered destroyed from a
collectable standpoint are now becoming worth a second look for repair and
restoration. While they will never command the value and respect of their
unmolested brethren, properly restored these instruments can easily become
valuable enough to justify the work required.
Guitars that have
been played a long time will often have some ill conceived repairs and
modifications and will have often been refinished many times. Our candidate
here is no exception. It is a late 50’s- early 60’s Fender Stratocaster.
It has been cut out for humbuckers, has had a
fulcrum tremolo installed as a floater, and some control cavity mods. While a
majority of this would be hidden under the pick guard, having the single coil
pickups floating in these large cavities is not going to be good for tone. Then
of course there is still the issue of the tremolo.
Upon thorough
examination of the body I noted these additional problems. All the pickup
cavities had routed deeper into the body than they should have.
Also, due to the many
haphazard re-finishes, the body is now .095” thinner than it should be. The
control cavity mod, most likely to add a 4th pot, has a section that
is routed at different depths and an odd little wire channel cut in the top.
Thankfully the neck pocket,
output jack cut out and tremolo spring cavity had not been altered. The body
arrived at my shop with a majority of the screw holes plugged and some layout
lines scribed in pencil onto the top.
While the
customer’s request was to restore the body to a state ready for a period solid
color finish, he also wanted a repair that would not “ghost” through the
finish. As most of these bodies are made from three planks joined together it
quickly became apparent that the best course of action was to replace part or
all of the top of the center plank. This would actually be easier than the
standard “bathtub” type repair and as a bonus possibly allow a tri-tone burst
finish if desired.
The first step is
to lay out the area to be replaced. Unfortunately the pickup cavities extend
beyond the center plank by about 1/4” on the bass side as shown by the
straightedge.
This will
not however be noticeable from the top. There was also no need to remove the
entire top of the center plank and doing so would have taken me into the output
jack cavity so I opted to only remove what I needed on the treble side. The
area to be removed is carefully laid out with blue masking tape.
As you can see, there will
still be some additional work at the control cavity, but replacing this one
piece of wood will take care of 95% of our problems.
To make a good
straight, square, clean opening I needed a template. So a square hole was cut
into a piece of 1/2” MDF that was exactly 1/8” wider than the area I laid out
and a few inches longer than needed. The hole was carefully cut on my table
saw. This was aligned over the area I marked out and it and the body were
clamped to a workboard at my bench.
I installed a 5/8” guide bushing and a 1/2” spiral bit in my plunge
router providing the desired 1/16” clearance to match my lay out. Since the
opening in my template was wider than my router base could span I needed a way
to support the router during the cut to keep it from tipping in and ruining the
cut. A strip of 1/4” plywood with a hole drilled through the center was placed
over the bushing and secured with a few pieces of two sided tape.
After making a few dry runs to check my
tool path, slightly repositioning my clamps until I was confident there was no
interference it was time to start cutting. I double and triple checked my
clamps to make sure they would not slip and began. The material was removed in
1/8” lifts, cutting around the perimeter first and then wasting out the center.
The entire area was cut down
just far enough to provide a completely clean surface for the repair to be
glued to.
Well almost,
there are those little terraces over by the control cavity to deal with.
Cutting down to that depth would have left me scary thin over the tremelo
spring cavity. Since there is more work over there anyway, we will take care of
them in a slightly different manner.
By repositioning my
template I could cut out the top of the control cavity to the same depth and
square it up to the rest of the repair.
This left me with one area still slightly deeper which I will simply
fit a small piece into and glue up with the rest of the repair. The body was
kept clamped to my workboard until I was ready to glue in the new pieces. This
was to avoid any warpage that might occur from removing so much of the center
piece and exposing all this fresh wood to the air.
Now it’s time to
prep the new piece of wood to be glued in. This is an Alder body so a plank of
Alder with similar grain orientation was chosen. Both the body and the donor
plank were left in my shop to acclimate. They were carefully monitored by
weight to gauge their moisture content. Both pieces need to be at equilibrium
and in stasis prior to any work being done otherwise the repair will fail. To
aide in obtaining the best possible grain match, I marked out the grain of the
missing piece on a piece of scratch paper and used that as a guide to help
select the portion of the plank to be used.
Also take note of the dent left by the strap
button on the end, this will need attention as it will be a problem when we
trim off our repair.
The cut out was
prepped lightly with a hard sanding block to knock down any small ridges and
tool tracks. Our new piece was carefully cut and planed to size, paying close
attention to the grain that will be seen on the top. Getting the grain to run
out the same and appear evenly spaced where it meets the original wood is key
to making the repair as unnoticeable as possible. Proper fitment of the piece
is also critical for a stable repair that does not “ghost” later. The new piece
should be able to be pressed into place completely with moderate hand pressure
but need to be tapped out with a mallet. Great care must be exercised here. Try
fitting a piece to tight and the body may split, to loose and the repair will
be unstable. When tapping the piece back out during fit up one must also be
very careful not to chip out any of the wood.
Once I was happy
with the fit all mating surfaces were given a light coat of Titebond, both in
the body and on the new piece. The key is in getting the amount of glue just
right. Too little and the joint will be weak and the work overall less stable.
Too much and not only have you made more cleanup work but you run the risk of
locking the joint up hydraulically, preventing the new piece from seating
properly and again having a weak and less stable repair. While I could have
most likely used my go-bars to clamp this in place, I felt more comfortable
using an array of clamps with the body held in a vise.
This allowed me to peek in the tremolo cavity and be
sure the new plank was seating properly everywhere and not just at the end and
to clean up any squeeze out in there while it was soft rather than try to deal
with it when dried. The following day I removed the clamps and fitted and glued
the remaining pieces needed at the top of the control cavity. This was done with a clamp and a few small
spruce spring bars.
The new wood was intentionally left
about 1/32” proud of the original surface and to run long at the end by about a
1/8”. A few strokes with a jack plane brought the new wood down to the proper
level quickly. I would rather plane down the new piece than run the risk of
having it wind up low, especially in light of the fact that this body was
already a bit thin. Using a bottom bearing flush cut bit in my router the end
was trimmed back using the original body as a guide. The strap button hole
mentioned earlier was filled in prior to this, otherwise the pilot bearing
would have dropped into it and left a big ugly divot in the end of the plank I
just put in. After that I could restore the armrest bevel across the new wood
using my jack plane. A little work with my sanding blocks and it’s ready to
have all its cavities routed out to specs.
Using My
Stratocaster template all the cavities are routed in with a carbide spiral cut
bit, again working in 1/8” lifts. The holes were drilled for mounting the
standard tremolo bridge and for the ground wire to the spring cavity. A final
sanding with 180 grit and we are done.
Our body is now as close to factory spec at the time of manufacture as
it can be. Even the grain match on the new piece of alder is pretty good
There are still some minor
chips and dings that the finisher will need to take care of but once it’s finished and all put back
together it will take a good eye and a close inspection to find the repair.
www.brianhowardguitars.com
www.brianhowardguitars.com
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